Preview

Pinnacle Airlines Flight 3701

Powerful Essays
Open Document
Open Document
1344 Words
Grammar
Grammar
Plagiarism
Plagiarism
Writing
Writing
Score
Score
Pinnacle Airlines Flight 3701
Pinnacle Airlines
Flight 3701
N8396A

On October 14th 2004 Captain Jesse Rhodes and First Officer Peter Cesarz were transferring an empty CRJ 200 from Little Rock to Minneapolis. They ended up crashing 2.5 miles from the runway in Jefferson City, Missouri. Several Human Factors lead to the eventual crash and death of everyone on board.

Flight 3701 Departed Little Rock at 2121. Four hundred and fifty feet above the ground they pulled 2 G’s which caused the stick shakers to activate. The pilots were obviously out to see what this jet could do since there were no other souls on board. Their planned altitude was thirty three thousand feet for the remainder of the flight. While climbing to that altitude around fifteen thousand feet they pulled 2.3 g’s and had a ten thousand feet per minute rate of climb, which caused the stick shakers to activate for a second time. Once again they pulled back and climbed at nine thousand feet and pulled 1.87 g’s at twenty five thousand feet. Around 2135 they requested to climb to forty one thousand feet which is the service ceiling of the aircraft. (NTSB)

While climbing to the new altitude the airspeed dropped from 203 knots to 160 knots while they were climbing to forty one thousand feet from thirty seven thousand feet. The airspeed of 160 is very close to the stalling speed of the aircraft. Around this stalling speed the captain told the first officer that they will be coming down in a second and then stated that this thing will not hold altitude. The engines started to spool down and the stick shaker and stick pusher were activated three times in a ten second interval. The airplane then entered an aerodynamic stall. Once the stall occurred a left rolling motion began which eventually ended up in an eighty two degree left wing down configuration. At this time both of the engines actually flamed out. The captain declared an emergency at this time but only admitted to one of the engines failing, not both of them.

The two

You May Also Find These Documents Helpful

  • Good Essays

    Ubt1 Task 1

    • 1382 Words
    • 6 Pages

    duration of flight. “Double Wing” for example did not fly very far but seemed to float down to the…

    • 1382 Words
    • 6 Pages
    Good Essays
  • Satisfactory Essays

    Bulk Street: A Summary

    • 326 Words
    • 2 Pages

    On 12-15-2016, at approximately 1341 hours, I was notified by Cpl. Graves of a traffic crash at 3420 Bulk Street. The crash occurred at the Kinder-Morgan fuel terminal, within the Port of Tampa at approximately 1313 hours.…

    • 326 Words
    • 2 Pages
    Satisfactory Essays
  • Powerful Essays

    Case Briefing

    • 774 Words
    • 4 Pages

    At Los Angeles International Airport, a horrible accident by a continental DC-10 took place On March 1, 1978. According to some continental airlines experts the reason behind the accident was “two tires burst on the left landing gear”1. Despite the efforts of the captain to stop the plane, it was too late to control a plan that ran off the ramp with at 85 miles per hour. As a result “The landing gear broke through the tarmac, burrowed into the ground, and was ripped from the wing, making a 3.7 foot hole which allowed fuel to pour from the wing fuel tanks. The plane was severely damaged by the resulting fire and rendered unrepeatable”2.…

    • 774 Words
    • 4 Pages
    Powerful Essays
  • Good Essays

    Crash Course in Density

    • 438 Words
    • 2 Pages

    fuel pumps had failed. The worst possible news, they were out of fuel. In a…

    • 438 Words
    • 2 Pages
    Good Essays
  • Good Essays

    The flight was a short flight took off from Concord, NC and it was heading to Martinsville, VA. After a missed approach to land at the Martinsville/Blue Ridge Airport the Beech King Air 200 crashed into the a mount in Stuart VA. There were multiple causes that lead to the crash. The main factor was human error. The flight crew made devastating mistakes that lead to the crash and the death of both the pilot, copilot, and the eight passengers. The two mistakes that the crew made were lack of communication and operating a vehicle while under the influence of narcotics. While at the time the crew probably did not think they were making a mistake their actions in the end resulted in the crash.…

    • 735 Words
    • 3 Pages
    Good Essays
  • Good Essays

    The L-8 Blimp

    • 983 Words
    • 4 Pages

    On the morning of August 16, 1942, the L-8 was sent out on its morning voyage. On board were two men, first was Lieutenant Ernest Dewitt Cody, a very experienced pilot with many hours in the L-8. Next was Ensign Charles Ellis Adams who was brand new to the job. That morning mechanic J Riley Hill, started to prepare the L-8 for its flight. As he did his walk around everything looked fine to him, and perfectly in tact. At six o’clock in the morning, they departed from Treasure Island in the San Francisco Bay, leaving behind their…

    • 983 Words
    • 4 Pages
    Good Essays
  • Satisfactory Essays

    Southwest Flight 345

    • 451 Words
    • 2 Pages

    This was the first trip the flight crew had flown together and it was the second leg of the trip. The first officer had previous operational experience at LGA, including six flights in 2013. The captain reported having flown into LGA twice, including the accident flight, serving as the pilot monitoring for both flights.…

    • 451 Words
    • 2 Pages
    Satisfactory Essays
  • Powerful Essays

    Dunn, R. D., Jr. (1995, December 18). Pilot, crew of flight 1572 did their best (Statewide Edition). Hartford Courant, A.14. Hartford, Conn: Hartford Courant. (Document ID: 22945376).…

    • 2974 Words
    • 12 Pages
    Powerful Essays
  • Satisfactory Essays

    Uss Indianapolis

    • 718 Words
    • 3 Pages

    He was able to aft on the starboard side, although badly injured, he didn't get to the main engine room, No. 2 engine room, where he found No. 2 engine had lost vacuum and that was shut down. He did talk to somebody in No. 1 engine room. They told him that apparently the main steamline going through the port side of the forward engine room had been knocked loose. They had no steam and asked for instructions.…

    • 718 Words
    • 3 Pages
    Satisfactory Essays
  • Satisfactory Essays

    Why 880 Men Die

    • 462 Words
    • 2 Pages

    Indianapolis. The sinking of the ship was one of the worst day in history for the navy.…

    • 462 Words
    • 2 Pages
    Satisfactory Essays
  • Good Essays

    Imo was heading out of the harbour while Mont Blanc was heading in. The Mont Blanc was carrying 2,653 tonnes of heavy artillery, ammunition and other explosives. The Imo was moving too fast and sailing in the wrong side of the harbour. The Imo’s captain was trying to avoid a tugboat. He did not see the fast approaching Mont Blanc. Both ships blew their whistles as a warning, but neither ship moved out of the way until the last second. The Imo crashed…

    • 555 Words
    • 3 Pages
    Good Essays
  • Good Essays

    Malaysia Airlines’ Flight 370 Disappearance Have you ever pondered about a plane disappearing in the 21st century and not being able to find it? On March 8th, 2014 Malaysia Airlines Flight 370 disappeared. The plane was scheduled to take off from Kuala Lumpur, Malaysia and to land in Beijing, China. The flight held 227 passengers and 12 crew members. It is said that Flight 370 lost contact with air traffic control after less than an hour of flying.…

    • 514 Words
    • 3 Pages
    Good Essays
  • Powerful Essays

    Nasa

    • 3413 Words
    • 14 Pages

    "Space Shuttle Columbia Disaster." Wikipedia. Wikimedia Foundation, 05 Sept. 2012. Web. 17 May 2012. .…

    • 3413 Words
    • 14 Pages
    Powerful Essays
  • Good Essays

    Some books say the ship was blown off course, others blame an “error in navigation.”…

    • 775 Words
    • 4 Pages
    Good Essays
  • Better Essays

    Hypoxia

    • 1320 Words
    • 4 Pages

    Listening to this again, it’s clear that there are missing segments. There is no order from atc to descend to 11k, probably because they did it in a way that did not comply with anyone's procedures; their memory is affected, still groggy. Incapacitated copilot wondering why they are at 11k and running out of fuel? That is reality.…

    • 1320 Words
    • 4 Pages
    Better Essays